Performance evaluation of reduced-chord rotor blading as applied to J73 two-stage turbine 4: over-all performance of first-stage turbine with reduced-chord rotor blades at inlet conditions of 35 inches of mercury absolute and 700 R (open access)

Performance evaluation of reduced-chord rotor blading as applied to J73 two-stage turbine 4: over-all performance of first-stage turbine with reduced-chord rotor blades at inlet conditions of 35 inches of mercury absolute and 700 R

Report presenting a study of the first stage performance characteristics of the two-stage turbine from the J73 turbojet engine. The reduced-chord first-stage turbine operated at a peak brake internal efficiency of over 91 percent at a stage overall pressure ratio of 1.4 and at 90 percent of the design equivalent speed. The unit exhibited high efficiency over a wide range of operating variables.
Date: July 5, 1957
Creator: Schum, Harold J.
System: The UNT Digital Library
Performance evaluation of reduced-chord rotor blading as applied to J73 two-stage turbine 5: effect of inlet pressure on over-all performance at design speed and inlet temperature of 700 degrees R (open access)

Performance evaluation of reduced-chord rotor blading as applied to J73 two-stage turbine 5: effect of inlet pressure on over-all performance at design speed and inlet temperature of 700 degrees R

Report presenting an investigation of a reduced-chord multistage turbine at design speed and various turbine-inlet pressures from 12 to 40 inches of mercury absolute. At each inlet pressure, the turbine was operated over a range of overall turbine total-pressure ratios; turbine-inlet temperature was maintained at 700 degrees R. The results indicated that no appreciable effect on turbine overall performance was observed over the range of turbine-inlet total pressures investigated.
Date: July 5, 1957
Creator: Schum, Harold J.
System: The UNT Digital Library
Phase III Absorber Rod Sample Irradiation. Irradiation Request ORNL-MTR-28 (open access)

Phase III Absorber Rod Sample Irradiation. Irradiation Request ORNL-MTR-28

None
Date: July 5, 1957
Creator: Leitten, C. F. Jr.
System: The UNT Digital Library
Studies on Large Area Sub-Fabric Burns (open access)

Studies on Large Area Sub-Fabric Burns

The detonation of shot one at Bikini Atoll on March 1, 1954, produced a fallout of radioactive ash upon Rongelap Atoll, Marshall Islands. The distribution of the radioactive ash on the islands and in the plants and animals of the area has been studied and evaluated. During the first expedition to Rongelap Atoll on March 26, 1954, biological samples were collected and measurements made of the radiation contamination. On three additional expeditions extensive collections of material were made for this study, the last on January 25-30, 1955. The decline in radioactivity was measured in 1499 samples of fish, invertebrates, land plants, algae, birds, plankton, soil, and water from the Rongelap area. During this study particular emphasis was placed upon evaluation of the radioactivity in food used by the natives. Coconut milk collected on March 26, 1954, contained 1.03 microcuries per kilogram of wet tissue while the coconut meat had 1.16 mu c/kg. By January 25-30, 1955, the level in coconut milk had declined to 0.041 mu c/kg and the meat to 0.036 mu c/ kg. Fish muscle on March 26, 1954, averaged 2.74 mu c/kg and fish liver 204.0 mu c/kg. The decline to January 25-30 was 0.10 mu c/kg …
Date: July 5, 1957
Creator: Berkley, K. M. & Pearse, H. E.
System: The UNT Digital Library
Transonic Flutter Investigation of a Cantilevered, Aspect-Ratio-4, 45 Degree Sweptback, Untapered Wing With Three Different Pylon-Mounted External Store Configurations (open access)

Transonic Flutter Investigation of a Cantilevered, Aspect-Ratio-4, 45 Degree Sweptback, Untapered Wing With Three Different Pylon-Mounted External Store Configurations

Report presenting an investigation of the transonic flutter characteristics of a cantilevered, aspect-ratio-4, 45 degree sweptback, untapered wing with three different pylon-mounted external-store configurations. An additional study was created during the investigation to find a store configuration with a substantially higher flutter speed than what was obtained with the other two stores. Results regarding general comments, the investigation of store types A and B, node-line survey, and the investigation of store type C are provided.
Date: July 5, 1957
Creator: Ruhlin, Charles L. & Boswinkle, Robert W., Jr.
System: The UNT Digital Library
Wind-Tunnel Tests of the Static Longitudinal Characteristics at Low Speed of a Swept-Wing Airplane With Blowing Flaps and Leading-Edge Slats (open access)

Wind-Tunnel Tests of the Static Longitudinal Characteristics at Low Speed of a Swept-Wing Airplane With Blowing Flaps and Leading-Edge Slats

Memorandum presenting a wind-tunnel investigation of a high-wing airplane with an aspect ratio 6.75 wing with approximately 36 degrees of sweepback in order to determine the lift effectiveness obtainable with trailing-edge blowing flaps in combination with leading-edge slats. Close to theoretical flap effectiveness was obtained with blowing flaps deflected 45, 55, and 65 degrees at low angles of attack. Results regarding the wind tunnel, take-off performance, landing performance, and comparisons with flight data are provided.
Date: July 5, 1957
Creator: James, Harry A. & Maki, Ralph L.
System: The UNT Digital Library
Wind-tunnel tests of the static longitudinal characteristics at low speed of a swept-wing airplane with blowing flaps and leading-edge slats (open access)

Wind-tunnel tests of the static longitudinal characteristics at low speed of a swept-wing airplane with blowing flaps and leading-edge slats

Report presenting a wind-tunnel investigation of a high-wing airplane with an aspect ratio 6.75 wing with approximately 36 degrees of sweepback to determine the lift effectiveness obtainable with trailing-edge blowing flaps in combination with leading-edge slats. Flap effectiveness and stability were maintained to high angles of attack by control of leading-edge flow separation with slats. An analysis of the take-off performance, landing performance, and comparisons with flight data are provided.
Date: July 5, 1957
Creator: James, Harry A. & Maki, Ralph L.
System: The UNT Digital Library