HOT CELL DEMONSTRATION OF ZIRFLEX AND SULFEX PROCESSES. Report No. 3 (open access)

HOT CELL DEMONSTRATION OF ZIRFLEX AND SULFEX PROCESSES. Report No. 3

ABS>Hot cell demonstration of the Zirflex decladding process coupled with a modified Purex solvent extraction process was completed using specimens of Zircaloy-clad UO/sub 2/ irradiated to levels of 6150-14,600 Mwd/TU. Soluble losses of uranium and plutonium to the decladding solutions were about 0.05%. Centrifugation of the decladding solution is probably necessary to remove up to 1% of the UO/sub 2/ present as fines resulting from the fracture of low (93 to 95%) density pellets; high (96%) density pellets produced few fines. Approximately 5 hours were required to dissolve the UO/sub 2/ core material (14,000 Mwd/TU) in 4M HNO/sub 3/ versus 6 to 7 hours for unirradiated pellets to produce a solvent extraction feed of 100 g U/l and 3M HNO/sub 3/. Gamma decontamination factors for uranium in the Purex CU stream and plutonium in the BP stream were increased by factors of 2 to 10 from the normal 1.3 x 10/sup 3/ and 2.1 x 10/sup 3/, respectively, by pretreatment of the solvent extraction feed with dincetyl monoxime or its degradation product, oxalic acid. Preliminary data indicate radiation damage degrades the solvent, 30% TBP diluted with Amsco 125- 82, upon one pass through the mixer-settler banks with feed solutions irradiated …
Date: May 14, 1962
Creator: Goode, J.H. & Baillie, M.G.
System: The UNT Digital Library
SNAP-50 reactor development program (open access)

SNAP-50 reactor development program

None
Date: May 14, 1962
Creator: unknown
System: The UNT Digital Library
Stress Analysis of the PM-2A Reactor Vessel (open access)

Stress Analysis of the PM-2A Reactor Vessel

The stress analysis performed on the PM-2A reactor vessel and cover is discussed. The maximum combined stress (51,000 psi) occurred in the studs after reaching steady-state conditions. A fatigue analysis indicated that this stress could be safely applied 2500 times, and since the studs do not approach 2500 cycles from initial stud tightening to steady-state conditions, they should not suffer any fatigue damage. (auth)
Date: May 14, 1962
Creator: Rowekamp, B. J.; McLaughlin, D. W.; Chittum, R. A. & Aitken, C. C.
System: The UNT Digital Library