Serial/Series Title

Georgia-Pacific: Crossett Mill Identifies Heat Recovery Projects and Operational Improvements that May Save $9.6 Million Annually (open access)

Georgia-Pacific: Crossett Mill Identifies Heat Recovery Projects and Operational Improvements that May Save $9.6 Million Annually

An assessment team conducted a mill-wide energy survey at Georgia-Pacific's Crossett, Arkansas mill to update a previous pinch analysis. Three heat recovery projects were identified that could reduce annual costs by $4.8 million and reduce natural gas use by 1,845,000 x 106 Btu. The overall payback period for the heat recovery projects would be less than 1 year. Furthermore, by implementing operational improvements, the mill could save $4.8 million more annually and 1,500,000 x 106 Btu in natural gas.
Date: November 1, 2003
Creator: unknown
System: The UNT Digital Library
Ohio Aluminum Industries: Compressed Air System Improvement Project Saves Energy and Improves Product Quality (open access)

Ohio Aluminum Industries: Compressed Air System Improvement Project Saves Energy and Improves Product Quality

In 2001, Ohio Aluminum Industries implemented the first phase of a compressed air system improvement project at its Cleveland, Ohio, plant. By completing this phase, the plant stabilized the system's pressure and improved its performance. Furthermore, it yielded annual energy savings of 716,000 kilowatt-hours and $73,200. The total cost for the project's first phase was $83,500, making the simple payback slightly more than 1 year.
Date: November 1, 2003
Creator: United States. Department of Energy. Office of Energy Efficiency and Renewable Energy. Office of Industrial Technologies.
System: The UNT Digital Library
American Water Heater Company: Compressed Air System Optimization Project Saves Energy and Improves Production at Water Heater Plant (open access)

American Water Heater Company: Compressed Air System Optimization Project Saves Energy and Improves Production at Water Heater Plant

In 2001, American Water Heater Company implemented a system-level improvement project on the compressed air system that serves its manufacturing plant in Johnson City, Tennessee. The plant now operates with less compressor capacity, which has reduced its energy consumption and maintenance needs. The project's total cost was $228,000. The annual compressed air energy savings (2,345,000 kWh) and maintenance savings total $160,000, yielding a simple payback of 17 months. Furthermore, the system now supports the plant's production processes more effectively, which has improved product quality and increased production.
Date: November 1, 2003
Creator: United States. Department of Energy. Office of Energy Efficiency and Renewable Energy. Office of Industrial Technologies.
System: The UNT Digital Library