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Response of Dual-Purpose Reinforced-Concrete Mass Shelter (open access)

Response of Dual-Purpose Reinforced-Concrete Mass Shelter

BS>A reinforced-concrete dual-purpose underground parking garage and personnel sheiter designed for a long-duration incident pressure of 40 psi was tested. The sheiter was exposed to shot Priscilla, an approximately 37-kt 700-ft balloon burst (June 24, 1957), at a ground range of 1600 ft (predicted 35-psi peak incident-pressure level). The recorded peak incident pressure at the shelter was approximately 39 psi. Postshot soil borings were made to obtain undisturbed samples for determining soil characteristics. Preshot and postshot field surveys were made to determine the total lateral and vertical displacement of the structure. The test structure provided adequate protection from the effects of the test device at the test GZ distance. Despite failure of the door sealing gasket, a rise in pressure in the interior did not exceed 1.0 psi. The flat-slab roof and supporting structure were more than adequate to resist the 39psi peak incident test loading. (P.C.H.)
Date: April 1, 1961
Creator: Cohen, E.; Laing, E. & Bottenhofer, A.
System: The UNT Digital Library
Test of Buried Structural-Plate Pipes Subjected to Blast Loading (open access)

Test of Buried Structural-Plate Pipes Subjected to Blast Loading

From abstract: Two 20-ft-long 7-ft-diameter 10-gauge structural-plate pipes, having longitudinal joints with eight bolts per foot, were buried and tested in the Smoky event of Operation Plumbbob at predicted pressure levels of 195 and 265 psi. The depth of burial was 10 ft over the crown of the pipe.
Date: July 28, 1961
Creator: Williamson, R. A. & Huff, P. H.
System: The UNT Digital Library